Some semblance of Normal

When I last wrote, there was a long list of things that weren’t working/going well. The broken tow bar, roof leak, mashed fender, etc.

Well, the tow bar seems to be working fine. The roof isn’t leaking despite unusually heavy and frequent rain where we are staying (more on where later). Oh, the third RVlock was also having issues. I diagnosed it that the bar that operates the latch was bent. Once I straightened it, the lock has worked fine.

I had spent some time looking for body shops for thefront left fender damage RV – but there simply wasn’t anything out here. Not that we wanted to be out of the RV for the week it probably would take to fix it. The last fender we had repaired (much less damage from some lady in a gas station) took two days, and then we had to go back for the Diamond Shield. Thus we chose to do the repairs myself. Click -> to see the detailed damage.

I had done a lot of bodywork in my life – but mostly the kind where Bondo is being used to smooth out damaged metal. This repair job was fiberglass that had 10 breaks. One of the things I discovered when I took a better look at the fender was there was a large crack in the lower middle – where nothing hit it. Looking behind I could see there was a fiberglass patch, poorly installed in that area either at the factory or where the front cap was made. Lots of Bondo had been put on the outside of the front cap as well.  The twisting stress from the accident caused the damaged area to open up.

I reviewed my “fiberglass repair skills” on YouTube. It really CAN be a good resource so long as one is discerning. Time to order supplies: TotalBoat epoxy, mixing cups and sticks, small cheap brushes for application, a good mouse electric sander, a supply of sandpaper for the mouse as well as for hand sanding. I ordered two different thicknesses of fiberglass (single layer and mat), and a large duffle bag to put all that and some additional tools I would need. I had no place to store all this when it was raining, so I put a tarp under the front of the RV and I’d push the bag underneath when I wasn’t working.

Oh, and I tried several goo removers – the RV has Diamond Sheild on the lower front; a dense plastic film that is supposed to limit rock chip damage.  It can be peeled off with a little heat but leaves a nasty glue behind that almost nothing dissolves (I even tried gasoline, which did work).  Several hours went into a tedious cycle of application, waiting for the goo remover to work, then scraping.  In some cases the goo was simply sanded away, sacrificing sandpaper in the process.

When fiberglass breaks, the edges shred. It is like when cardboard is torn – it won’t go all the way back together, so each of the breaks needed to be cleaned up so the pieces could be put back in the correct place.   I first sanded down the inside and outside edges to give the epoxy clean access to the underlying fiberglass.  Then I ran a hacksaw blade between the damaged edges to cut off some of the frayed fiberglass so the sides would fit back into their proper alignment.  

Also, there is a metal U-channel support behind the fender that was “glued” across the joint between the front cap and the fender. It took me about 6 sessions of several hours each to straighten the support, clean up the torn edges, and epoxy the damaged sections together.  inside view of fiberglass repairsOn the back, I used mostly the thick fiberglass mat and epoxy to reinforce the damaged areas. On the front side, I added multiple narrow strips of single-layer fiberglass across the cracks.  Once everything had been reconstructed, work then moved on to Bondo and spot putty to smooth the outer surface.  I used a combination of a metal ruler and my hand to identify low spots; marking them with a pencil and then adding filler.  I used a foot-long 1×2 with sandpaper wrapped to even out everything.  Once I could see that this process was going to lead to a satisfactory repair, I ordered paint from PaintScratch.com. Their database was incomplete – I had to choose several different years of Tiffin motorhomes to find the three different paint codes I needed. I also ordered some primer and clear coat paint. With this automotive-style paint, the colors are sprayed on in multiple light coats.  Then when finished a clear coat is applied (in a similar manner) which is then polished to a shiny finish. PaintScratch supplied 12-ounce spray cans whose sprayers worked surprisingly well.

I think the one thing I failed to get was a better quality masking tape as I had some issues with the stripes – paint leaking under the tape.  I had to respray a number of edges to get clean lines. The most time was spent trying to get the surface as smooth and clean as possible. Some of the smaller defects didn’t show up until the first layer of finish paint was applied.

 

 

 

 

 

 

The headlight is now reinstalled and several layers of clear coat have been applied, but the surface is still “too orange peel” and needs further work (at the next long-term RV park, hopefully).

To recap – our insurance probably would have covered this repair, minus a $500 deductible.  Our rates surely would have gone up.  I spent less than that buying paint, tools, and supplies.  And most importantly, we didn’t have to leave our RV for a week to get it repaired. 

In other news – we have been working at Henry’s Lake State Park in Idaho.  It is only about 20 miles from West Yellowstone and thus Yellowstone National Park.  For three days (each) of light and sometimes interesting work a week, we get a full hookup site – and coincidentally a place to work on a broken fender.  

We’ve made a number of trips to Yellowstone as well as other local parks.  That is another advantage of this arrangement, 4 days off a week and lots of time to explore.  We even climbed Mt Washburn in Yellowstone.  

Oh, and two small doggies will be joining us soon.  Pictures and names coming in the next blog. 

 

On the road again, sort of.

Before I unwind my tale – let me mention D and W campground outside Champaign Illinois.  They are just off I-57 and Marketplace.  They are a family owned and operated campground.  It has a nice spring fed lake and lots of trees.  The grounds are well maintained including the roads.  It is a great place to stay overnight or for months.

We are back on the road, sort of.  We spent several months near our home base – working on landscaping, selling stuff from the house, giving away more and lots of other chores.  We plan to sell the house next year, so there is so much downsizing to do.  We sold our electric bikes and bought a new pair we liked better.  Then there was the sump drainpipe that needed expensive repair work and the new computer we hope will extend the life of the very old laptop I type these blogs on.  We are both photographers and edit pictures and videos.

We also replaced the shade motors on the windshield sun and night shades.  The night shade started acting wonky, stopping in the wrong place, refusing to reprogram. I found the motors on Amazon.  When I went to replace them, I found two things.  There is a brown wire that is supposed to be connected ignition so the night shade can’t be lowered too far while driving.  It was connected only to thin air.  No ignition wire to be found nearby.  The other thing I found; as I was untangling the cables – one spade connector on the night shade (the one with the problem) just fell off as it wasn’t crimped well.  So, both motors were replaced and went into storage as they might just be ok.

We traveled north to Wisconsin to spend a week with family – then will head back to home base for a week for one last medical test before we head out west.

Of course, every trip has its problems.  When we left the campground that we had been at for a couple of months, everything worked fine.  The slide even worked several times when we were there (we pull in the main slide whenever we have storm winds forecasted in the 60 mph range).

We pull into our Wisconsin park and neither the jacks nor the main hydraulic slide would work.  Now we had problems previously with the HWH hydraulic system and I ended up replacing both of the solenoids mounted on the pump system.  And the repair seemed to work.  It did work for a short trip and several uses while parked.

But when we arrived, the leveling panel was dark and nothing, even the emergency push buttons wouldn’t work.  Big Sigh…..  When we pushed the extend button for the main slide, it moved out just a little and that was it.  Basically – the hydraulic controller released the pressure holding the slide cylinder in and it moved on its own.  I jumped power directly to the hydraulic motor and the slide extended.  I think we were just lucky on that.

After looking through what HWH hydraulic diagrams I had, I went looking for a 5-amp fuse – and found one inside the dash.  Blown.  Wonderful place Tiffin.  When I replaced it, the leveling control panel powered up.  That panel talks to a controller (included in the front left storage bay) via a CAN bus and that controller talks to the hydraulic valve controller mounted with the pump.

There are two solenoids at the pump.  The MASTER solenoid provides power to the valve control body mounted on top of the pump AND provides power to the second solenoid.  The MASTER solenoid is turned on any time Ignition is on.  This along with the controller and the dash panel let you know if the jacks are in Travel Mode – or not, whenever you are driving.  However, that means that the MASTER solenoid must be a Continuous Duty solenoid – one that can stay energized for long periods of time.  If you just to go Amazon and order a 12V solenoid it likely is an intermittent version – like what you might use for a

intermittent solenoid used continuously: burnt wires.
intermittent solenoid used continuously: burnt wires.

starter.  I had mistakenly replaced my MASTER with just such a solenoid, and it did not survive the 7-hour trip between campgrounds.  I had a spare intermittent solenoid that I installed temporarily, and everything worked.  And I ordered a new, Continuous Duty solenoid that will be installed before our return trip.

Great – that is solved or will be once the correct solenoid arrives from Amazon.  Moving on – before we left home base, we purchased a new TPMS system.  The RVIBrake system got to be too big a hassle.  We bought a TST 507 with 10 sensors.  I went to program the sensors into the display – and they wouldn’t load in.  I tried multiple times.  I replaced a couple of sensor batteries just in case.  I watched four different Youtube videos on how to program these things and read two different instruction manuals on the process.  I was doing everything just exactly how it was shown.  Hold the sensor next to the bottom left side of the display, hit the GO button……  Nope, nadda, zilch…. So, I watched again, and again and realized that they often hit the go button first, then as the sensor got near the display, pop, the serial number was read.  When I tried mine, the serial number read – TWO inches away from the display.  Being too close, the signal must have been too hot to read properly.  I went on to load all 10 sensors and install them on the RV and pickup truck.

The TPMS worked on the way up to Wisconsin but a couple were a little flakey and as I suspected, the batteries weren’t new.  As I was replacing the batteries in the sensors, I noticed oil on the left rear wheel rim of the RV.  The axle seal was leaking…..  More videos.  With the F53, the entire wheel/brake disk/hub assembly freewheels on bearings on the end of the transaxle body.  A half shaft slides through the hub, into the transaxle, mating with a spline into the planetary gears and bolts to the outside of the hub.  Transaxle oil floods that space and is sealed in – with a paper gasket where the half-shaft bolts to the hub. Apparently leaks there is a thing with F53 transaxles.  The only socket wrench I had with me was an 8 inch 3/8ths drive. I put that on – and what were supposed to be 180 lb-ft tightened nuts moved with only moderate force.  Also, apparently insufficiently torqued axle flange bolts is also a thing with F53 transaxles.  There are Youtube videos showing people finding paper seals blown out, falling apart etc.  Mine were in place, so I bought a breaker bar and tightened all the nuts.  I cleaned up all the oil, so I could tell if it leaks again – added some oil to the transaxle (was only a little low).  Then I checked the other side too – loose but not leaking.

We are headed back to home base in less than a week – I’ll keep an eye on it and if it leaks, I’ll have to replace the seal.

A week at home base, then head west young man (and woman).