When does it end?

Before we start,  I DO like to travel.  Normally.  Of course, when I happen to be the person on the front line when something breaks, traveling can be a bit stressful.  I sometimes sit there and think: “Is that a new noise?”  It’s been nearly a year since the engine blow-up but there has been a constant string of little to medium-sized issues.

In my last post, I referred to a rear axle flange leak – that I tightened the nuts and cleaned up the oil.  We drove back toward our home base and checked – and yes, it was still leaking.  But before that- this week+ has been one thing after another.  So here we start…..

I started both researching the axle leak problem and looking for a seal.  I found several posts and videos where DIYers took care of their F53 axle flange leaks.  More on that below.  The immediate issue was where to get a new gasket in just over a week we would be stationary.  No online place either had one or could get one to us in less than two weeks.  I hit up my local Ford dealer and they promised to get one (I always order two) delivered in a few days – and they did.

Our 2019 Tiffin is based on a Ford F53 stripped chassis.  This chassis seems to come with one of three different transaxles.  None of the numbers on the transaxle seemed to match up with anything I could find on the Internet.  Most references were for 8-stud axle flanges.  Mine had twelve.  Aside from the issue of getting the right gasket, the torque values for the various flange stud nuts is very different based on the size of the studs (6 or 8 studs flanges use larger diameter and higher torque values than the twelve).

I had never dealt with this size of transaxle before.  The F53 has dual wheels on the rear.  The hub on each side, to which the wheels bolt and the brake disk attach connects to the transaxle via a pair of bearings.  Without the axle shaft installed, the hub would free wheel.  F53 12 Bolt axle flangeA “half axle” then inserts through the hub and a spline shaft connects with the gearing inside the transaxle.  The Flange on the end of the half-axle bolts to the hub, and thus drives it.  There is a thin paper gasket that seals transaxle oil from leaking between the flange and the hub.

The transaxle is filled with oil high enough that it runs out to the bearings in the hubs.  I let oil out of the transaxle case so I didn’t have to deal with a lot of oil running out when I pulled the axle.  There are three plugs in the case – one at the bottom to fully drain, one part way up the side for a partial drain and one higher up which is the fill and full-measure port.  The case is vented, so if you pull the plug on the middle port, it will drain and drain quite fast.  I let oil run out, until it slowed a bit and put the plug back in.  My estimate was it was low enough to minimize the oil that would come out later (it did).

The process goes something like this: place the RV on a flat surface, with wheel chocks in place.  During removal and re-installation you will need to release the parking brake and place transmission in neutral. Remove the hub cover (the left side has left-hand threads).  Mark the flange and hub, so that when reassembling, you can line everything up the same way.  Remove the flange nuts.  Now release the brake and go to neutral.  The flange should pull out fairly easily if all pressure on the drive system has been removed.

I cleaned up both sides (hub and flange).  I removed the remainder of the gasket with a utility knife and buffed up the surfaces with 3M green scrubber and did a final cleaning with a paper towel wetted with brake cleaner.  I applied the gasket dry (as per instructions).  The axle slid back in and with a little bump and jockeying, it mated in just the same place it came out.

The service manual specified to tighten the nuts in a star pattern – that is start with one nut – then go opposite (180 degrees), then 90 degrees, then another 180.  Or based on a clock, noon, 6, 9 and 3.  Then move to the next set and tighten in the same order.  With twelve bolts, that meant three sets of 4.  I snugged by hand, then set the torque wrench to 20, 40, and 65, in turn, following the pattern each time.  Finally, I cleaned up the hub, hub cover and wheel with brake cleaner so that if anything leaked again, I could easily tell.

After installing the cover, I added back new gear oil (my service manual spec’d 75W140.  It took 6 pints – it all depends on how much yours leaked and how much drained out.

We were waiting to leave town for one last medical test on me (which turned out good).  We headed northwest, into Iowa, and stayed the first night at a Harvest Host (Alpaca Farm).  It was our second trip to that host and it was as great as the first time.  It was hot during the day, but by evening it was cool enough to sleep with the windows open.  The next day was a long one – 6 plus hours on the road.  The axle flange didn’t leak – that was great.

Debbie and I weren’t really in sync that day.  We were having issues with gas stations.  Flying J and Pilot stations were limiting credit card purchases to $100, even in the RV lanes.  You can’t fill up an 80-gallon tank on $100 unless you travel back to the 1960’s.  AND, when I put my card in again, the station, or the card company denies your charge – EVEN IF I PUT IN A DIFFERENT CARD!!! So we pull into the left RV lane and there are bags on the left pumps – the easiest one to use.  But there are pumps on the right side of that lane – so I try that – “processing” forever.  (AND there was a deep puddle I had to wade to get to asshole parking in the waythe right pump – wet shoes!)  Ok, the right lane is now empty – so Deb drives around the lot to enter the right lane but some bozo parked his RV and trailer in the way, forcing a tighter turn into the right lane.  I was worried about the truck jumping the curb, as was Deb.  We weren’t agreeing on when to turn which way.  Deb was halfway into the lane when I in frustration said,”Just pull up, I’ll tell you when to stop” – when I heard a crunch.  front left fender damageThe left front fender hit the island guard that was sticking WAY THE HELL OUT INTO THE GAS LANE.  Shit!  To add insult to injury, this lane didn’t like my card either so I had to walk into the station to prepay.  Oh, and some stations put a $500 hit on my account, which is adjusted later to the actual amount – all the while limiting the

 exact same purchase to $100.  After filling up, we pulled out of the lane and parked in the lot to add half a roll of tape to the fender.  Some Flying J’s just plain suck rocks.  Others are great.  This one obviously sucked boulders!!

Update:  I am fixing this myself.  I’ve done lots of body work and paint, but very little fiberglass before.  The fiberglass broke in about 10 places.  Trying to work through insurance and finding a place to get the work done quickly (likely to be in a shop for a week or more) – we just couldn’t see doing that.  I’m almost through with the fiberglass work.  Then finish it out with glazing, primer, and paint.  It turns out I can get the same BASF paint in two different spray options.  We shall see.

When we pulled into our RV park – the girl was “new and on her own”.  She assigned us a site but we found a large fifth wheel parked there.  Back to the office – and a new site – backed in – but found only 30 amp service.  Back again – assigned another site and it had a very antiquated and jury-rigged 50 amp, but it worked.  Then the fun begins.  While unhitching the pickup truck, I found something wrong with the RoadMaster Nighthawk tow bar.  I couldn’t get the hitch to catch in the storage position.  It was sticking out too far and wouldn’t recess.  I presumed something in the stinger was broken and the bar was about to separate.  That wouldn’t be good.

Of course, I didn’t have the correct socket, so we went out and bought one and some supplies in case I could put it back together. Nighthawk repair I managed to remove the nut (inside the stinger) that held the tow bar in and couldn’t, for the longest time, figure out what was supposed to be there.  The nut I removed was trying its best to slide out of the stinger so there had to be a washer, spring, or something in there originally, that had broken into pieces and fallen out of the stinger.

nighthawk repairI couldn’t find any diagram of the internals of the stinger.  I finally decided there was a washer missing.  So, a trip to Menards was on the schedule for 6 am the next morning.  And wonder of wonders, I found a grade 8 washer there that was exactly the right size – and a better-fitting socket.  Back home – lubricate and reassemble it all, install on Rover and we are ready to leave and water starts dripping out of the speaker just overhead of the driver.  We had downpours much of the night.  I opened up the back of the cabinet but couldn’t directly identify the leak (it’s way overhead).  I went on the roof and dried off the area but could not find any break in the sealants.  Out of frustration, I coated all the seams in the area with self-leveling sealant.  Won’t know if it worked until it rains again – which seems to be coming soon. (It rained cats, dogs, and elephants at the next park, and no leak. Yea!!!)

We found a park today that had vacancies for three days.  A little relaxation is in order.

Mike

P.S. THE DAMN RVLOCK DOESN”T WORK EITHER!!!!

On the road again, sort of.

Before I unwind my tale – let me mention D and W campground outside Champaign Illinois.  They are just off I-57 and Marketplace.  They are a family owned and operated campground.  It has a nice spring fed lake and lots of trees.  The grounds are well maintained including the roads.  It is a great place to stay overnight or for months.

We are back on the road, sort of.  We spent several months near our home base – working on landscaping, selling stuff from the house, giving away more and lots of other chores.  We plan to sell the house next year, so there is so much downsizing to do.  We sold our electric bikes and bought a new pair we liked better.  Then there was the sump drainpipe that needed expensive repair work and the new computer we hope will extend the life of the very old laptop I type these blogs on.  We are both photographers and edit pictures and videos.

We also replaced the shade motors on the windshield sun and night shades.  The night shade started acting wonky, stopping in the wrong place, refusing to reprogram. I found the motors on Amazon.  When I went to replace them, I found two things.  There is a brown wire that is supposed to be connected ignition so the night shade can’t be lowered too far while driving.  It was connected only to thin air.  No ignition wire to be found nearby.  The other thing I found; as I was untangling the cables – one spade connector on the night shade (the one with the problem) just fell off as it wasn’t crimped well.  So, both motors were replaced and went into storage as they might just be ok.

We traveled north to Wisconsin to spend a week with family – then will head back to home base for a week for one last medical test before we head out west.

Of course, every trip has its problems.  When we left the campground that we had been at for a couple of months, everything worked fine.  The slide even worked several times when we were there (we pull in the main slide whenever we have storm winds forecasted in the 60 mph range).

We pull into our Wisconsin park and neither the jacks nor the main hydraulic slide would work.  Now we had problems previously with the HWH hydraulic system and I ended up replacing both of the solenoids mounted on the pump system.  And the repair seemed to work.  It did work for a short trip and several uses while parked.

But when we arrived, the leveling panel was dark and nothing, even the emergency push buttons wouldn’t work.  Big Sigh…..  When we pushed the extend button for the main slide, it moved out just a little and that was it.  Basically – the hydraulic controller released the pressure holding the slide cylinder in and it moved on its own.  I jumped power directly to the hydraulic motor and the slide extended.  I think we were just lucky on that.

After looking through what HWH hydraulic diagrams I had, I went looking for a 5-amp fuse – and found one inside the dash.  Blown.  Wonderful place Tiffin.  When I replaced it, the leveling control panel powered up.  That panel talks to a controller (included in the front left storage bay) via a CAN bus and that controller talks to the hydraulic valve controller mounted with the pump.

There are two solenoids at the pump.  The MASTER solenoid provides power to the valve control body mounted on top of the pump AND provides power to the second solenoid.  The MASTER solenoid is turned on any time Ignition is on.  This along with the controller and the dash panel let you know if the jacks are in Travel Mode – or not, whenever you are driving.  However, that means that the MASTER solenoid must be a Continuous Duty solenoid – one that can stay energized for long periods of time.  If you just to go Amazon and order a 12V solenoid it likely is an intermittent version – like what you might use for a

intermittent solenoid used continuously: burnt wires.
intermittent solenoid used continuously: burnt wires.

starter.  I had mistakenly replaced my MASTER with just such a solenoid, and it did not survive the 7-hour trip between campgrounds.  I had a spare intermittent solenoid that I installed temporarily, and everything worked.  And I ordered a new, Continuous Duty solenoid that will be installed before our return trip.

Great – that is solved or will be once the correct solenoid arrives from Amazon.  Moving on – before we left home base, we purchased a new TPMS system.  The RVIBrake system got to be too big a hassle.  We bought a TST 507 with 10 sensors.  I went to program the sensors into the display – and they wouldn’t load in.  I tried multiple times.  I replaced a couple of sensor batteries just in case.  I watched four different Youtube videos on how to program these things and read two different instruction manuals on the process.  I was doing everything just exactly how it was shown.  Hold the sensor next to the bottom left side of the display, hit the GO button……  Nope, nadda, zilch…. So, I watched again, and again and realized that they often hit the go button first, then as the sensor got near the display, pop, the serial number was read.  When I tried mine, the serial number read – TWO inches away from the display.  Being too close, the signal must have been too hot to read properly.  I went on to load all 10 sensors and install them on the RV and pickup truck.

The TPMS worked on the way up to Wisconsin but a couple were a little flakey and as I suspected, the batteries weren’t new.  As I was replacing the batteries in the sensors, I noticed oil on the left rear wheel rim of the RV.  The axle seal was leaking…..  More videos.  With the F53, the entire wheel/brake disk/hub assembly freewheels on bearings on the end of the transaxle body.  A half shaft slides through the hub, into the transaxle, mating with a spline into the planetary gears and bolts to the outside of the hub.  Transaxle oil floods that space and is sealed in – with a paper gasket where the half-shaft bolts to the hub. Apparently leaks there is a thing with F53 transaxles.  The only socket wrench I had with me was an 8 inch 3/8ths drive. I put that on – and what were supposed to be 180 lb-ft tightened nuts moved with only moderate force.  Also, apparently insufficiently torqued axle flange bolts is also a thing with F53 transaxles.  There are Youtube videos showing people finding paper seals blown out, falling apart etc.  Mine were in place, so I bought a breaker bar and tightened all the nuts.  I cleaned up all the oil, so I could tell if it leaks again – added some oil to the transaxle (was only a little low).  Then I checked the other side too – loose but not leaking.

We are headed back to home base in less than a week – I’ll keep an eye on it and if it leaks, I’ll have to replace the seal.

A week at home base, then head west young man (and woman).